Plausibility Study of Hecto Pressure Ratio Concepts in Large Civil Aero-EnginesSource: Journal of Engineering for Gas Turbines and Power:;2018:;volume( 140 ):;issue: 005::page 51201DOI: 10.1115/1.4038124Publisher: The American Society of Mechanical Engineers (ASME)
Abstract: Enabling high overall pressure ratios (OPR), wave rotors, and piston concepts (PCs) seem to be solutions surpassing gas turbine efficiency. Therefore, a comparison of a wave rotor and three PCs relative to a reference gas turbine is offered. The PPCs include a Wankel, a two-stroke reciprocating engine, and a free piston. All concepts are investigated with and without intercooling. An additional combustion chamber (CC) downstream the piston engine is investigated, too. The shaft power chosen corresponds to large civil turbofans. Relative to the reference gas turbine, a maximum efficiency increase of 11.2% for the PCs and 9.8% for the intercooled wave rotor is demonstrated. These improvements are contrasted by a 5.8% increase in the intercooled reference gas turbine and a 4.2% increase due to improved gas turbine component efficiencies. Intercooling the higher component efficiency gas turbine leads to a 9.8% efficiency increase. Furthermore, the study demonstrates the high difference between intercooler and piston engine weight and a conflict between PC efficiency and chamber volume, highlighting the need for extreme lightweight design in any piston engine solution. Improving piston engine technology parameters is demonstrated to lead to higher efficiency, but not to a chamber volume reduction. Heat loss in the piston engines is identified as the major efficiency limiter.
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contributor author | Klein, Felix | |
contributor author | Staudacher, Stephan | |
date accessioned | 2019-02-28T10:57:41Z | |
date available | 2019-02-28T10:57:41Z | |
date copyright | 11/21/2017 12:00:00 AM | |
date issued | 2018 | |
identifier issn | 0742-4795 | |
identifier other | gtp_140_05_051201.pdf | |
identifier uri | http://yetl.yabesh.ir/yetl1/handle/yetl/4251192 | |
description abstract | Enabling high overall pressure ratios (OPR), wave rotors, and piston concepts (PCs) seem to be solutions surpassing gas turbine efficiency. Therefore, a comparison of a wave rotor and three PCs relative to a reference gas turbine is offered. The PPCs include a Wankel, a two-stroke reciprocating engine, and a free piston. All concepts are investigated with and without intercooling. An additional combustion chamber (CC) downstream the piston engine is investigated, too. The shaft power chosen corresponds to large civil turbofans. Relative to the reference gas turbine, a maximum efficiency increase of 11.2% for the PCs and 9.8% for the intercooled wave rotor is demonstrated. These improvements are contrasted by a 5.8% increase in the intercooled reference gas turbine and a 4.2% increase due to improved gas turbine component efficiencies. Intercooling the higher component efficiency gas turbine leads to a 9.8% efficiency increase. Furthermore, the study demonstrates the high difference between intercooler and piston engine weight and a conflict between PC efficiency and chamber volume, highlighting the need for extreme lightweight design in any piston engine solution. Improving piston engine technology parameters is demonstrated to lead to higher efficiency, but not to a chamber volume reduction. Heat loss in the piston engines is identified as the major efficiency limiter. | |
publisher | The American Society of Mechanical Engineers (ASME) | |
title | Plausibility Study of Hecto Pressure Ratio Concepts in Large Civil Aero-Engines | |
type | Journal Paper | |
journal volume | 140 | |
journal issue | 5 | |
journal title | Journal of Engineering for Gas Turbines and Power | |
identifier doi | 10.1115/1.4038124 | |
journal fristpage | 51201 | |
journal lastpage | 051201-10 | |
tree | Journal of Engineering for Gas Turbines and Power:;2018:;volume( 140 ):;issue: 005 | |
contenttype | Fulltext |