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    Forced Response Reduction of a Blisk by Means of Intentional Mistuning

    Source: Journal of Engineering for Gas Turbines and Power:;2019:;volume( 141 ):;issue: 001::page 11008
    Author:
    Beirow, Bernd
    ,
    Kühhorn, Arnold
    ,
    Figaschewsky, Felix
    ,
    Bornhorn, Alfons
    ,
    Repetckii, Oleg V.
    DOI: 10.1115/1.4040715
    Publisher: The American Society of Mechanical Engineers (ASME)
    Abstract: The effect of intentional mistuning has been analyzed for an axial turbocharger blisk with the objective of limiting the forced response due to low engine order excitation (LEO). The idea behind the approach was to increase the aerodynamic damping for the most critical fundamental mode in a way that a safe operation is ensured without severely losing aerodynamic performance. Apart from alternate mistuning, a more effective mistuning pattern is investigated, which has been derived by means of optimization employing genetic algorithms. In order to keep the manufacturing effort as small as possible, only two blade different geometries have been allowed, which means that an integer optimization problem has been formulated. Two blisk prototypes have been manufactured for purpose of demonstrating the benefit of the intentional mistuning pattern identified in this way: A first one with and a second one without employing intentional mistuning. The real mistuning of the prototypes has been experimentally identified. It is shown that the benefit regarding the forced response reduction is retained in spite of the negative impact of unavoidable additional mistuning due to the manufacturing process. Independently, further analyzes have been focused on the robustness of the solution by considering increasing random structural mistuning and aerodynamic mistuning as well. The latter one has been modeled by means of varying aerodynamic influence coefficients (AIC) as part of Monte Carlo simulations. Reduced order models have been employed for these purposes.
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      Forced Response Reduction of a Blisk by Means of Intentional Mistuning

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    http://yetl.yabesh.ir/yetl1/handle/yetl/4256434
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    contributor authorBeirow, Bernd
    contributor authorKühhorn, Arnold
    contributor authorFigaschewsky, Felix
    contributor authorBornhorn, Alfons
    contributor authorRepetckii, Oleg V.
    date accessioned2019-03-17T10:56:16Z
    date available2019-03-17T10:56:16Z
    date copyright9/14/2018 12:00:00 AM
    date issued2019
    identifier issn0742-4795
    identifier othergtp_141_01_011008.pdf
    identifier urihttp://yetl.yabesh.ir/yetl1/handle/yetl/4256434
    description abstractThe effect of intentional mistuning has been analyzed for an axial turbocharger blisk with the objective of limiting the forced response due to low engine order excitation (LEO). The idea behind the approach was to increase the aerodynamic damping for the most critical fundamental mode in a way that a safe operation is ensured without severely losing aerodynamic performance. Apart from alternate mistuning, a more effective mistuning pattern is investigated, which has been derived by means of optimization employing genetic algorithms. In order to keep the manufacturing effort as small as possible, only two blade different geometries have been allowed, which means that an integer optimization problem has been formulated. Two blisk prototypes have been manufactured for purpose of demonstrating the benefit of the intentional mistuning pattern identified in this way: A first one with and a second one without employing intentional mistuning. The real mistuning of the prototypes has been experimentally identified. It is shown that the benefit regarding the forced response reduction is retained in spite of the negative impact of unavoidable additional mistuning due to the manufacturing process. Independently, further analyzes have been focused on the robustness of the solution by considering increasing random structural mistuning and aerodynamic mistuning as well. The latter one has been modeled by means of varying aerodynamic influence coefficients (AIC) as part of Monte Carlo simulations. Reduced order models have been employed for these purposes.
    publisherThe American Society of Mechanical Engineers (ASME)
    titleForced Response Reduction of a Blisk by Means of Intentional Mistuning
    typeJournal Paper
    journal volume141
    journal issue1
    journal titleJournal of Engineering for Gas Turbines and Power
    identifier doi10.1115/1.4040715
    journal fristpage11008
    journal lastpage011008-8
    treeJournal of Engineering for Gas Turbines and Power:;2019:;volume( 141 ):;issue: 001
    contenttypeFulltext
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