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    Optimization of a 900 mm Tilting-Pad Journal Bearing in Large Steam Turbines by Advanced Modeling and Validation

    Source: Journal of Engineering for Gas Turbines and Power:;2019:;volume( 141 ):;issue: 002::page 21033
    Author:
    Mermertas, Ümit
    ,
    Hagemann, Thomas
    ,
    Brichart, Clément
    DOI: 10.1115/1.4041116
    Publisher: The American Society of Mechanical Engineers (ASME)
    Abstract: Modernization of steam turbine components can extend power plant lifetime, decrease maintenance costs, increase service intervals, and improve operational flexibility. However, this can also lead to challenging demands for existing components such as bearings, e.g., due to increased rotor weights. Therefore, a careful design and evaluation process of bearings is of major importance. This paper describes the applied advanced modeling methods and performed validation for the optimization of a novel 900 mm three-pad tilting pad journal bearing that showed high temperature sensitivity to the fresh oil supply temperature. The bearing was developed to cope with increased rotor weights within the low pressure (LP) steam turbine modernization at two 1000 MW nuclear power plants. With a static load of 2.7 MN at a speed of 1500 rpm, it represents one of the highest loaded applications for tilting pad bearings in turbomachinery worldwide. After identification of the reasons for the sensitivity, advanced modeling methods were applied to optimize the bearing. For this purpose, a more comprehensive bearing model was developed considering the direct lubrication at the leading pad edge and pad deformation. The results of the entire analyses indicated modifications of bearing clearances, pad length, thickness, and pivot position. The optimized bearing was then implemented on both units and proved its excellent operational behavior at increased fresh oil supply temperatures of up to 55 °C. In conclusion, the application of advanced modeling methods proved to be the key success factor in the optimization of this bearing, which represents an optimal solution for turbomachinery.
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      Optimization of a 900 mm Tilting-Pad Journal Bearing in Large Steam Turbines by Advanced Modeling and Validation

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    http://yetl.yabesh.ir/yetl1/handle/yetl/4256259
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    contributor authorMermertas, Ümit
    contributor authorHagemann, Thomas
    contributor authorBrichart, Clément
    date accessioned2019-03-17T10:40:49Z
    date available2019-03-17T10:40:49Z
    date copyright10/29/2018 12:00:00 AM
    date issued2019
    identifier issn0742-4795
    identifier othergtp_141_02_021033.pdf
    identifier urihttp://yetl.yabesh.ir/yetl1/handle/yetl/4256259
    description abstractModernization of steam turbine components can extend power plant lifetime, decrease maintenance costs, increase service intervals, and improve operational flexibility. However, this can also lead to challenging demands for existing components such as bearings, e.g., due to increased rotor weights. Therefore, a careful design and evaluation process of bearings is of major importance. This paper describes the applied advanced modeling methods and performed validation for the optimization of a novel 900 mm three-pad tilting pad journal bearing that showed high temperature sensitivity to the fresh oil supply temperature. The bearing was developed to cope with increased rotor weights within the low pressure (LP) steam turbine modernization at two 1000 MW nuclear power plants. With a static load of 2.7 MN at a speed of 1500 rpm, it represents one of the highest loaded applications for tilting pad bearings in turbomachinery worldwide. After identification of the reasons for the sensitivity, advanced modeling methods were applied to optimize the bearing. For this purpose, a more comprehensive bearing model was developed considering the direct lubrication at the leading pad edge and pad deformation. The results of the entire analyses indicated modifications of bearing clearances, pad length, thickness, and pivot position. The optimized bearing was then implemented on both units and proved its excellent operational behavior at increased fresh oil supply temperatures of up to 55 °C. In conclusion, the application of advanced modeling methods proved to be the key success factor in the optimization of this bearing, which represents an optimal solution for turbomachinery.
    publisherThe American Society of Mechanical Engineers (ASME)
    titleOptimization of a 900 mm Tilting-Pad Journal Bearing in Large Steam Turbines by Advanced Modeling and Validation
    typeJournal Paper
    journal volume141
    journal issue2
    journal titleJournal of Engineering for Gas Turbines and Power
    identifier doi10.1115/1.4041116
    journal fristpage21033
    journal lastpage021033-10
    treeJournal of Engineering for Gas Turbines and Power:;2019:;volume( 141 ):;issue: 002
    contenttypeFulltext
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    DSpace software copyright © 2002-2015  DuraSpace
    نرم افزار کتابخانه دیجیتال "دی اسپیس" فارسی شده توسط یابش برای کتابخانه های ایرانی | تماس با یابش
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