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    Experimental Study of Thermo-Acoustic Instability Triggering in a Staged Liquid Fuel Combustor Using High-Speed OH-PLIF

    Source: Journal of Engineering for Gas Turbines and Power:;2018:;volume( 140 ):;issue: 008::page 81505
    Author:
    Renaud, Antoine
    ,
    Tachibana, Shigeru
    ,
    Arase, Shuta
    ,
    Yokomori, Takeshi
    DOI: 10.1115/1.4038915
    Publisher: The American Society of Mechanical Engineers (ASME)
    Abstract: A staged injector developed by JAXA and fueled with kerosene is studied in a high-pressure combustion experiment. With a stable pilot fuel flow rate, the fuel flow rate in the main stage is progressively increased. A high-speed OH-planar laser-induced fluorescence (PLIF) system is used to record the flame motion at 10,000 fps. In the beginning of the recording, the flame behavior is dominated by relatively low-frequency rotation due to the swirling motion of the flow. These rotational motions then coexist with a thermo-acoustic instability around 475 Hz which increases the amplitude of the pressure fluctuations inside the chamber. Dynamic mode decomposition (DMD) analyses indicate that this instability is associated with a widening of the flame occurring when the pressure fluctuations are the highest, giving the instability a positive feedback. The instability frequency then abruptly switches to 500 Hz, while the mode shape remains the same. This frequency change is studied using time–frequency analysis to highlight a change in the feedback mechanism characterized by a modification of the time delay between pressure and heat release fluctuations.
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      Experimental Study of Thermo-Acoustic Instability Triggering in a Staged Liquid Fuel Combustor Using High-Speed OH-PLIF

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    http://yetl.yabesh.ir/yetl1/handle/yetl/4251284
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    contributor authorRenaud, Antoine
    contributor authorTachibana, Shigeru
    contributor authorArase, Shuta
    contributor authorYokomori, Takeshi
    date accessioned2019-02-28T10:58:14Z
    date available2019-02-28T10:58:14Z
    date copyright5/2/2018 12:00:00 AM
    date issued2018
    identifier issn0742-4795
    identifier othergtp_140_08_081505.pdf
    identifier urihttp://yetl.yabesh.ir/yetl1/handle/yetl/4251284
    description abstractA staged injector developed by JAXA and fueled with kerosene is studied in a high-pressure combustion experiment. With a stable pilot fuel flow rate, the fuel flow rate in the main stage is progressively increased. A high-speed OH-planar laser-induced fluorescence (PLIF) system is used to record the flame motion at 10,000 fps. In the beginning of the recording, the flame behavior is dominated by relatively low-frequency rotation due to the swirling motion of the flow. These rotational motions then coexist with a thermo-acoustic instability around 475 Hz which increases the amplitude of the pressure fluctuations inside the chamber. Dynamic mode decomposition (DMD) analyses indicate that this instability is associated with a widening of the flame occurring when the pressure fluctuations are the highest, giving the instability a positive feedback. The instability frequency then abruptly switches to 500 Hz, while the mode shape remains the same. This frequency change is studied using time–frequency analysis to highlight a change in the feedback mechanism characterized by a modification of the time delay between pressure and heat release fluctuations.
    publisherThe American Society of Mechanical Engineers (ASME)
    titleExperimental Study of Thermo-Acoustic Instability Triggering in a Staged Liquid Fuel Combustor Using High-Speed OH-PLIF
    typeJournal Paper
    journal volume140
    journal issue8
    journal titleJournal of Engineering for Gas Turbines and Power
    identifier doi10.1115/1.4038915
    journal fristpage81505
    journal lastpage081505-9
    treeJournal of Engineering for Gas Turbines and Power:;2018:;volume( 140 ):;issue: 008
    contenttypeFulltext
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