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    Rigid Mode Vibration Control and Dynamic Behavior of Hybrid Foil–Magnetic Bearing Turbo Blower

    Source: Journal of Engineering for Gas Turbines and Power:;2017:;volume( 139 ):;issue: 005::page 52501
    Author:
    Jeong, Sena
    ,
    Jeon, Doyoung
    ,
    Lee, Yong Bok
    DOI: 10.1115/1.4034920
    Publisher: The American Society of Mechanical Engineers (ASME)
    Abstract: In this study, experimental and analytical analyses of the vibration stability of a 225 kW class turbo blower with a hybrid foil–magnetic bearing (HFMB) were performed. First, critical speed and unbalance vibration responses were examined as part of the rotordynamic research. Its shaft diameter was 71.5 mm, its total length was 693 mm, and the weight of the rotor was 17.8 kg. The air foil bearing (AFB) utilized was 50 mm long and had a 0.7 aspect ratio. In the experiments conducted, excessive vibration and rotor motion instability occurred in the range 12,000–15,000 rpm, which resulted from insufficient dynamic pressure caused by the length of the foil bearing being too short. Consequently, as the rotor speed increased, excessive rotor motion attributable to aerodynamic and bearing instability became evident. This study therefore focused on improving rotordynamic performance by rectifying rigid mode unstable vibration at low speed, 20,000 rpm, and asynchronous vibration due to aerodynamic instability by using HFMB with vibration control. The experimental results obtained were compared for each bearing type (AFB and HFMB) to improve the performance of the vibration in the low-speed region. The experimental results show that the HFMB technology results in superior vibration stability for unbalance vibration and aerodynamic instability in the range 12,000–15,000 rpm (200–250 Hz). The remarkable vibration reduction achieved from vibration control of the HFMB–rotor system shows that oil-free turbomachinery can achieve excellent performance.
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      Rigid Mode Vibration Control and Dynamic Behavior of Hybrid Foil–Magnetic Bearing Turbo Blower

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    http://yetl.yabesh.ir/yetl1/handle/yetl/4233690
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    contributor authorJeong, Sena
    contributor authorJeon, Doyoung
    contributor authorLee, Yong Bok
    date accessioned2017-11-25T07:15:49Z
    date available2017-11-25T07:15:49Z
    date copyright2016/22/11
    date issued2017
    identifier issn0742-4795
    identifier othergtp_139_05_052501.pdf
    identifier urihttp://138.201.223.254:8080/yetl1/handle/yetl/4233690
    description abstractIn this study, experimental and analytical analyses of the vibration stability of a 225 kW class turbo blower with a hybrid foil–magnetic bearing (HFMB) were performed. First, critical speed and unbalance vibration responses were examined as part of the rotordynamic research. Its shaft diameter was 71.5 mm, its total length was 693 mm, and the weight of the rotor was 17.8 kg. The air foil bearing (AFB) utilized was 50 mm long and had a 0.7 aspect ratio. In the experiments conducted, excessive vibration and rotor motion instability occurred in the range 12,000–15,000 rpm, which resulted from insufficient dynamic pressure caused by the length of the foil bearing being too short. Consequently, as the rotor speed increased, excessive rotor motion attributable to aerodynamic and bearing instability became evident. This study therefore focused on improving rotordynamic performance by rectifying rigid mode unstable vibration at low speed, 20,000 rpm, and asynchronous vibration due to aerodynamic instability by using HFMB with vibration control. The experimental results obtained were compared for each bearing type (AFB and HFMB) to improve the performance of the vibration in the low-speed region. The experimental results show that the HFMB technology results in superior vibration stability for unbalance vibration and aerodynamic instability in the range 12,000–15,000 rpm (200–250 Hz). The remarkable vibration reduction achieved from vibration control of the HFMB–rotor system shows that oil-free turbomachinery can achieve excellent performance.
    publisherThe American Society of Mechanical Engineers (ASME)
    titleRigid Mode Vibration Control and Dynamic Behavior of Hybrid Foil–Magnetic Bearing Turbo Blower
    typeJournal Paper
    journal volume139
    journal issue5
    journal titleJournal of Engineering for Gas Turbines and Power
    identifier doi10.1115/1.4034920
    journal fristpage52501
    journal lastpage052501-12
    treeJournal of Engineering for Gas Turbines and Power:;2017:;volume( 139 ):;issue: 005
    contenttypeFulltext
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    DSpace software copyright © 2002-2015  DuraSpace
    نرم افزار کتابخانه دیجیتال "دی اسپیس" فارسی شده توسط یابش برای کتابخانه های ایرانی | تماس با یابش
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