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    Stabilizing a 46 MW Multistage Utility Steam Turbine Using Integral Squeeze Film Bearing Support Dampers

    Source: Journal of Engineering for Gas Turbines and Power:;2015:;volume( 137 ):;issue: 005::page 52506
    Author:
    Ertas, Bugra
    ,
    Cerny, Vaclav
    ,
    Kim, Jongsoo
    ,
    Polreich, Vaclav
    DOI: 10.1115/1.4028715
    Publisher: The American Society of Mechanical Engineers (ASME)
    Abstract: A 46 MW 5500 rpm multistage single casing utility steam turbine experienced strong subsynchronous rotordynamic vibration of the first rotor mode; preventing full load operation of the unit. The root cause of the vibration stemmed from steam whirl forces generated at secondary sealing locations in combination with a flexible rotorbearing system. Several attempts were made to eliminate the subsynchronous vibration by modifying bearing geometry and clearances, which came short of enabling full load operation. The following paper presents experimental tests and analytical results focused on stabilizing a 46 MW 6230 kg utility steam turbine experiencing subsynchronous rotordynamic instability. The paper advances an integral squeeze film damper (ISFD) solution, which was implemented to resolve the subsynchronous vibration and allow full load and full speed operation of the machine. The present work addresses the bearingdamper analysis, rotordynamic analysis, and experimental validation through waterfall plots, and synchronous vibration data of the steam turbine rotor. Analytical and experimental results show that using ISFD improved the stability margin by a factor of 12 eliminating the subsynchronous instability and significantly reducing critical speed amplification factors. Additionally, by using ISFD the analysis showed significant reduction in interstage clearance closures during critical speed transitions in comparison to the hard mounted tilting pad bearing configuration.
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      Stabilizing a 46 MW Multistage Utility Steam Turbine Using Integral Squeeze Film Bearing Support Dampers

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    http://yetl.yabesh.ir/yetl1/handle/yetl/157949
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    contributor authorErtas, Bugra
    contributor authorCerny, Vaclav
    contributor authorKim, Jongsoo
    contributor authorPolreich, Vaclav
    date accessioned2017-05-09T01:17:50Z
    date available2017-05-09T01:17:50Z
    date issued2015
    identifier issn1528-8919
    identifier othergtp_137_05_052506.pdf
    identifier urihttp://yetl.yabesh.ir/yetl/handle/yetl/157949
    description abstractA 46 MW 5500 rpm multistage single casing utility steam turbine experienced strong subsynchronous rotordynamic vibration of the first rotor mode; preventing full load operation of the unit. The root cause of the vibration stemmed from steam whirl forces generated at secondary sealing locations in combination with a flexible rotorbearing system. Several attempts were made to eliminate the subsynchronous vibration by modifying bearing geometry and clearances, which came short of enabling full load operation. The following paper presents experimental tests and analytical results focused on stabilizing a 46 MW 6230 kg utility steam turbine experiencing subsynchronous rotordynamic instability. The paper advances an integral squeeze film damper (ISFD) solution, which was implemented to resolve the subsynchronous vibration and allow full load and full speed operation of the machine. The present work addresses the bearingdamper analysis, rotordynamic analysis, and experimental validation through waterfall plots, and synchronous vibration data of the steam turbine rotor. Analytical and experimental results show that using ISFD improved the stability margin by a factor of 12 eliminating the subsynchronous instability and significantly reducing critical speed amplification factors. Additionally, by using ISFD the analysis showed significant reduction in interstage clearance closures during critical speed transitions in comparison to the hard mounted tilting pad bearing configuration.
    publisherThe American Society of Mechanical Engineers (ASME)
    titleStabilizing a 46 MW Multistage Utility Steam Turbine Using Integral Squeeze Film Bearing Support Dampers
    typeJournal Paper
    journal volume137
    journal issue5
    journal titleJournal of Engineering for Gas Turbines and Power
    identifier doi10.1115/1.4028715
    journal fristpage52506
    journal lastpage52506
    identifier eissn0742-4795
    treeJournal of Engineering for Gas Turbines and Power:;2015:;volume( 137 ):;issue: 005
    contenttypeFulltext
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