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contributor authorE. Poursaeidi
contributor authorA. A. Pirmohammadi
contributor authorM. R. Mohammadi Arhani
date accessioned2017-05-09T00:32:38Z
date available2017-05-09T00:32:38Z
date copyrightJuly, 2009
date issued2009
identifier issn1528-8919
identifier otherJETPEZ-27075#042501_1.pdf
identifier urihttp://yetl.yabesh.ir/yetl/handle/yetl/140439
description abstractThis paper presents the outcomes of computational mechanics applied in the root-cause investigation on hot section failure of a 25 MW gas turbo generator in the domestic power plant after 2228 start-stops and 52,586 h operation. The failure includes the complete damage of the first and the second stage of nozzles, blades, seals, shroud segments, and also a peripheral damage on the disk of first stage. Several reported cases from the different power plants with similar events evidenced that the failure is a serious common type in the mentioned gas turbine engine. A previous study on complete metallurgical analysis of disk, moving blades, and lock-pins, was done by and (2008, “Failure Analysis of Lock-Pin in a Gas Turbine Engine,” Eng. Fail. Anal., 15(7), pp. 847–855), which concluded that the mechanical specification of applied materials had been satisfied. Nevertheless, some problems were found in the fractographic results of lock-pins: the typical fatigue fracture surfaces in the neck of failed lock-pins and frankly localized pitting signs near the head of lock-pin. The lock-pins are kinds of small devices that lock the buckets after inserting them into disk grooves. In this work, a 3D finite element model (FEM) of a blade, a disk, and a lock-pin are made and analyzed by the ANSYS software. The results of the FEM showed a reasonable agreement between the analysis and position of fracture on lock-pins. Also, the results showed that the second vibrational mode of the bucket is a possible cause of failure because in this mode the peak stress occurs on the head of the lock-pin. However, inadequate design and long time service reduced the performance of lock-pins for sustaining a severe hot condition in the first stage of the turbine section.
publisherThe American Society of Mechanical Engineers (ASME)
titleMechanical Investigation of a Failed Lock-Pin
typeJournal Paper
journal volume131
journal issue4
journal titleJournal of Engineering for Gas Turbines and Power
identifier doi10.1115/1.3077660
journal fristpage42501
identifier eissn0742-4795
keywordsLocks (Waterways)
keywordsStress
keywordsPins (Engineering)
keywordsGas turbines
keywordsTurbines
keywordsDisks
keywordsBlades
keywordsFailure AND Fatigue
treeJournal of Engineering for Gas Turbines and Power:;2009:;volume( 131 ):;issue: 004
contenttypeFulltext


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