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contributor authorBaoshi Chen
contributor authorTianyi Zhang
date accessioned2017-05-08T23:15:37Z
date available2017-05-08T23:15:37Z
date copyrightJanuary, 1983
date issued1983
identifier issn1528-8919
identifier otherJETPEZ-26779#125_1.pdf
identifier urihttp://yetl.yabesh.ir/yetl/handle/yetl/97135
description abstractTest results obtained from a two-stage fan are analysed and the reasons that caused the design performance target not to be attained are presented in this paper. Addition of a partspan shroud on rotor 1 caused higher losses and changed radial distribution of parameters. Modification on the flowpath and chord length of stator 1 resulted in excessively high inlet Mach number and flow separation in the hub region. The high load and high incidence at the hub of rotor 2 caused higher losses and reduced stall margin of the fan.
publisherThe American Society of Mechanical Engineers (ASME)
titlePerformance Analysis of the Test Results on a Two-Stage Transonic Fan
typeJournal Paper
journal volume105
journal issue1
journal titleJournal of Engineering for Gas Turbines and Power
identifier doi10.1115/1.3227372
journal fristpage125
journal lastpage129
identifier eissn0742-4795
keywordsMach number
keywordsStress
keywordsChords (Trusses)
keywordsDesign
keywordsRotors
keywordsFlow separation AND Stators
treeJournal of Engineering for Gas Turbines and Power:;1983:;volume( 105 ):;issue: 001
contenttypeFulltext


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