Investigation of a Pavement Premature Failure on a Weak and Moisture Susceptible BaseSource: Journal of Performance of Constructed Facilities:;2009:;Volume ( 023 ):;issue: 005Author:Dar-Hao Chen
DOI: 10.1061/(ASCE)CF.1943-5509.0000040Publisher: American Society of Civil Engineers
Abstract: An investigation was conducted to determine the root cause of the premature pavement failure. The premature pavement failure occurred in the form of rutting and alligator cracking. Although the affected portion was repaired by removing and replacing the top 75-mm asphalt concrete (AC), the repaired AC experienced recurring rutting and alligator cracking in a few weeks. Through extensive field and lab testing, it was found that the weak base is the root cause of the premature failure and the brittleness of the AC is secondary. However, both the base and AC were built according to plan and met the current material and field density requirements. It was concluded that density alone for construction quality control is not sufficient, as it was not able to protect against premature failures from occurring. Although there are many different ways to minimize premature failures, an immediate action is to include proof rolling in construction quality control. Proof rolling has been used with success to ensure proper compaction and to locate unstable areas, as the stability is greatly influenced by the degree of densification achieved during compaction.
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contributor author | Dar-Hao Chen | |
date accessioned | 2017-05-08T21:37:12Z | |
date available | 2017-05-08T21:37:12Z | |
date copyright | October 2009 | |
date issued | 2009 | |
identifier other | %28asce%29cf%2E1943-5509%2E0000043.pdf | |
identifier uri | http://yetl.yabesh.ir/yetl/handle/yetl/57628 | |
description abstract | An investigation was conducted to determine the root cause of the premature pavement failure. The premature pavement failure occurred in the form of rutting and alligator cracking. Although the affected portion was repaired by removing and replacing the top 75-mm asphalt concrete (AC), the repaired AC experienced recurring rutting and alligator cracking in a few weeks. Through extensive field and lab testing, it was found that the weak base is the root cause of the premature failure and the brittleness of the AC is secondary. However, both the base and AC were built according to plan and met the current material and field density requirements. It was concluded that density alone for construction quality control is not sufficient, as it was not able to protect against premature failures from occurring. Although there are many different ways to minimize premature failures, an immediate action is to include proof rolling in construction quality control. Proof rolling has been used with success to ensure proper compaction and to locate unstable areas, as the stability is greatly influenced by the degree of densification achieved during compaction. | |
publisher | American Society of Civil Engineers | |
title | Investigation of a Pavement Premature Failure on a Weak and Moisture Susceptible Base | |
type | Journal Paper | |
journal volume | 23 | |
journal issue | 5 | |
journal title | Journal of Performance of Constructed Facilities | |
identifier doi | 10.1061/(ASCE)CF.1943-5509.0000040 | |
tree | Journal of Performance of Constructed Facilities:;2009:;Volume ( 023 ):;issue: 005 | |
contenttype | Fulltext |