| contributor author | M. Uhre Pedersen | |
| contributor author | C. O. Clorius | |
| contributor author | L. Damkilde | |
| contributor author | P. Hoffmeyer | |
| date accessioned | 2017-05-08T21:14:52Z | |
| date available | 2017-05-08T21:14:52Z | |
| date copyright | August 1999 | |
| date issued | 1999 | |
| identifier other | %28asce%290887-3828%281999%2913%3A3%28107%29.pdf | |
| identifier uri | http://yetl.yabesh.ir/yetl/handle/yetl/44190 | |
| description abstract | In 1993 after 9 years of use, one of the wooden blades of a windmill was struck by lightning. After demounting, the damaged blade was handed over to the Technical University of Denmark, Lyngby, for the investigation of potential fatigue damage. This paper presents an experimental determination of the residual strength of the glued-in bolts that served as the blade to rotor hub connection in the windmill. The load history of the bolts, the test method, the observed fracture modes, and the force displacement curves are presented along with the recorded residual strength of the bolts. The bolts with a length of 500 mm had a special hollow tapering giving them a higher load-bearing capacity than solid bolts of equal dimensions. An FEM analysis confirms the higher load-bearing capacity. The mean residual stength was found to be 362 kN with a standard deviation of 37 kN, which is 95% of the predicted strength based on short-term tests on similar bolts. At fracture, a displacement between 0.4 and 1.0 mm was observed. In the majority of failures, the bolts were pulled out like a cork from a bottle. | |
| publisher | American Society of Civil Engineers | |
| title | Strength of Glued-In Bolts after Full-Scale Loading | |
| type | Journal Paper | |
| journal volume | 13 | |
| journal issue | 3 | |
| journal title | Journal of Performance of Constructed Facilities | |
| identifier doi | 10.1061/(ASCE)0887-3828(1999)13:3(107) | |
| tree | Journal of Performance of Constructed Facilities:;1999:;Volume ( 013 ):;issue: 003 | |
| contenttype | Fulltext | |