contributor author | Kaoshan Dai | |
contributor author | Yijian Yang | |
contributor author | Zhihong He | |
contributor author | Tao Li | |
contributor author | Peng Chen | |
contributor author | Jianze Wang | |
contributor author | Jun Xu | |
date accessioned | 2023-11-28T00:05:35Z | |
date available | 2023-11-28T00:05:35Z | |
date issued | 6/21/2023 12:00:00 AM | |
date issued | 2023-06-21 | |
identifier other | JPCFEV.CFENG-4477.pdf | |
identifier uri | http://yetl.yabesh.ir/yetl1/handle/yetl/4294054 | |
description abstract | This paper presents the investigation results of a base-isolated RC frame-shear wall structure located in Luding County, Sichuan Province, China, which was damaged by a Ms 6.8 earthquake on September 5, 2022. This recently constructed school office building was about 9 km away from the epicenter. The isolation layer of this building consists of 54 rubber bearings and 12 viscous dampers. These viscous dampers or their connections failed during the earthquake, and the limit state included connection breaking or global buckling of the damper. Also, the superstructure suffered some minor damage. To investigate the cause of structural damages, a nonlinear time-history analysis is conducted using the ground motions recorded by four seismic stations close to the building. The onsite investigation and numerical simulation results revealed the possible reasons for the failure. | |
publisher | ASCE | |
title | Postearthquake Investigation of a Base-Isolated Building in the 2022 Ms 6.8 Luding Earthquake | |
type | Journal Article | |
journal volume | 37 | |
journal issue | 5 | |
journal title | Journal of Performance of Constructed Facilities | |
identifier doi | 10.1061/JPCFEV.CFENG-4477 | |
journal fristpage | 04023037-1 | |
journal lastpage | 04023037-12 | |
page | 12 | |
tree | Journal of Performance of Constructed Facilities:;2023:;Volume ( 037 ):;issue: 005 | |
contenttype | Fulltext | |