Show simple item record

contributor authorSchäflein, Lukas
contributor authorJanssen, Johannes
contributor authorBrandies, Henri
contributor authorJeschke, Peter
contributor authorBehre, Stephan
date accessioned2023-08-16T18:10:49Z
date available2023-08-16T18:10:49Z
date copyright12/6/2022 12:00:00 AM
date issued2022
identifier issn0889-504X
identifier otherturbo_145_6_061004.pdf
identifier urihttp://yetl.yabesh.ir/yetl1/handle/yetl/4291565
description abstractIn this paper, we present the evaluation of the aerodynamic robustness to rim seal purge flow of an optimized 1.5-stage axial turbine configuration with a bowed stator profile and endwall contouring. Performance maps obtained by experiments and numerical simulations show that the efficiency benefit gained by this optimized configuration is partially reduced, but not eliminated, by the injection of purge flow through the cavity downstream of the first stator. Measurements with five-hole probes and hot-wire probes, as well as unsteady RANS simulations, give detailed insights into the physical effects of the purge flow inside the rotor passage. There, when no purge flow is injected, the optimized configuration diminishes the formation of loss-inducing secondary flow structures near the hub and the casing. When purge flow is injected, however, new strong secondary flow structures are induced near the hub. These vortices generate additional losses and thereby partially negate the efficiency benefits gained by the optimization. From the data, we found that this influence of the purge flow is limited to the lower half of the channel height. The data also show that the optimized configuration is able to reduce the vorticity near the casing regardless of the purge flow injection, which in turn leads to an efficiency increase in this area. Together, these effects lead to a reduction of the previously gained efficiency benefit by the optimized configuration when it is subjected to purge flow injection. However, compared to a baseline configuration with cylindrical endwalls also subject to purge flow injection, the overall efficiency is still increased by 0.38%.
publisherThe American Society of Mechanical Engineers (ASME)
titleInfluence of Purge Flow Injection on the Performance of an Axial Turbine With Three-Dimensional Airfoils and Non-Axisymmetric Endwall Contouring
typeJournal Paper
journal volume145
journal issue6
journal titleJournal of Turbomachinery
identifier doi10.1115/1.4056238
journal fristpage61004-1
journal lastpage61004-10
page10
treeJournal of Turbomachinery:;2022:;volume( 145 ):;issue: 006
contenttypeFulltext


Files in this item

Thumbnail

This item appears in the following Collection(s)

Show simple item record