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contributor authorGhada S. Ellithy
contributor authorTimothy D. Stark
date accessioned2022-01-30T21:52:36Z
date available2022-01-30T21:52:36Z
date issued12/1/2020 12:00:00 AM
identifier other%28ASCE%29GT.1943-5606.0002382.pdf
identifier urihttp://yetl.yabesh.ir/yetl1/handle/yetl/4268988
description abstractThis paper describes the application of unsaturated soil mechanics to an interstate connecting-ramp embankment that failed during construction. Specifically, matric suction is incorporated into the calculation of the tension crack (TC) depth induced by desiccation and strain incompatibility and the contribution of matric suction to embankment shear strength. The results are compared with field observations to assess the viability of unsaturated soil mechanics in modeling compacted embankments in stability analyses. Results from this study suggest that using unsaturated shear strength parameters while introducing a TC in the compacted fill yields a reasonable inverse analysis of this interstate embankment. This may be preferred in slope stability analyses to the current practice of using an undrained shear strength (i.e., cohesion) for the unsaturated compacted fill and including a TC to generate a reasonable factor of safety.
publisherASCE
titleCase Study: Unsaturated Embankment Failure on Soft Soils
typeJournal Paper
journal volume146
journal issue12
journal titleJournal of Geotechnical and Geoenvironmental Engineering
identifier doi10.1061/(ASCE)GT.1943-5606.0002382
page10
treeJournal of Geotechnical and Geoenvironmental Engineering:;2020:;Volume ( 146 ):;issue: 012
contenttypeFulltext


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