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contributor authorJenny, P.
contributor authorAbhari, R. S.
contributor authorRose, M. G.
contributor authorBrettschneider, M.
contributor authorEngel, K.
contributor authorGier, J.
date accessioned2017-05-09T01:03:51Z
date available2017-05-09T01:03:51Z
date issued2013
identifier issn0889-504X
identifier otherturb_135_05_051022.pdf
identifier urihttp://yetl.yabesh.ir/yetl/handle/yetl/153505
description abstractThe paper presents an experimental and computational study of the unsteady behavior of the rotor hub passage vortex in an axial lowpressure turbine. Different flow structures are identified as having an effect on the size, strength, shape, position, and the unsteady behavior of the rotor hub passage vortex. The aim of the presented study is to analyze and quantify the sensitivities of the different flow structures and to investigate their combined effects on the rotor hub passage vortex. Particular attention is paid to the effect of the rim seal purge flow and of the unsteady blade row interaction. The rotor under investigation has nonaxisymmetric end walls on both hub and shroud and is tested at three different rim seal purge flow injection rates. The rotor has separated pressure sides at the operating point under investigation. The nondimensional parameters of the tested turbine match real engine conditions. The 2sensor fast response aerodynamic probe (FRAP) technique and the fast response entropy probe (FENT) systems developed by ETH Zurich are used in this experimental campaign. Timeresolved measurements of the unsteady pressure, temperature and entropy fields between the rotor and stator blade rows are taken and analyzed. Furthermore, the results of URANS simulations are compared to the measurements and the computations are also used to detail the flow field. The experimental results show a 30% increase of the maximum unsteadiness and a 4% increase of the loss in the hub passage vortex per percent of injected rim seal cooling flow. Compared to a free stream particle, the rim seal purge flow was found to do 60% less work on the rotor.
publisherThe American Society of Mechanical Engineers (ASME)
titleUnsteady Rotor Hub Passage Vortex Behavior in the Presence of Purge Flow in an Axial Low Pressure Turbine
typeJournal Paper
journal volume135
journal issue5
journal titleJournal of Turbomachinery
identifier doi10.1115/1.4007837
journal fristpage51022
journal lastpage51022
identifier eissn1528-8900
treeJournal of Turbomachinery:;2013:;volume( 135 ):;issue: 005
contenttypeFulltext


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