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contributor authorClay Naito
contributor authorRichard Sause
contributor authorIan Hodgson
contributor authorStephen Pessiki
contributor authorThomas Macioce
date accessioned2017-05-08T21:34:52Z
date available2017-05-08T21:34:52Z
date copyrightJuly 2010
date issued2010
identifier other%28asce%29be%2E1943-5592%2E0000112.pdf
identifier urihttp://yetl.yabesh.ir/yetl/handle/yetl/56637
description abstractOn the evening of December 27, 2005 the fascia beam supporting the east side parapet wall of the third span of the Lake View Drive Bridge failed under the action of dead load. To gain insight into the potential causes of the failure a series of forensic analyses were conducted on the beams decommissioned from the bridge. The study correlates external observations of surface condition with internal chloride profile, depth of carbonation, and existing corrosion. The forensic investigation indicated that strand cover was reduced due to the construction methods of the time. The chloride level in the concrete at the lower layer of strands was high enough that corrosion would be expected. Chloride attack was identified to have come from the leakage of water between beams from the bridge deck surface above. Based on the research findings recommendations are made for visual inspection, and guidelines are provided for condition rating of noncomposite prestressed concrete box beam bridges.
publisherAmerican Society of Civil Engineers
titleForensic Examination of a Noncomposite Adjacent Precast Prestressed Concrete Box Beam Bridge
typeJournal Paper
journal volume15
journal issue4
journal titleJournal of Bridge Engineering
identifier doi10.1061/(ASCE)BE.1943-5592.0000110
treeJournal of Bridge Engineering:;2010:;Volume ( 015 ):;issue: 004
contenttypeFulltext


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