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contributor authorDar-Hao Chen
contributor authorZhiming Si
contributor authorMustafa Saribudak
date accessioned2017-05-08T21:15:28Z
date available2017-05-08T21:15:28Z
date copyrightApril 2009
date issued2009
identifier other%28asce%290887-3828%282009%2923%3A2%28100%29.pdf
identifier urihttp://yetl.yabesh.ir/yetl/handle/yetl/44602
description abstractA forensic study was conducted to investigate the premature pavement failure of heaving and cracking on the north bound lane of SH6 and to determine (1) the causes of the heaving and cracking; (2) the severity and extent of the problem; and (3) a prevention strategy. Ground penetration radar (GPR), falling weight deflectometer (FWD), dynamic cone penetrometer (DCP), and soil boring and laboratory tests were conducted. Soil maps provided by the Natural Resource Conservation Service (NRCS) and the electrical resistivity tomography (ERT) were utilized to locate areas that may have similar problems for the ongoing project. It was concluded that the heaving was caused by high organic content in soils. The low pH of the lime treated subgrade layer indicated that the lime stabilization was ineffective. This was due to the high concentration of organic matter. FWD and DCP results indicated that the heaved/cracked areas are losing structural load support. Approximately 84% of the bumps/dips detected by the profiler were also detected by the GPR. Based on the GPR results, it was estimated that about
publisherAmerican Society of Civil Engineers
titleRoadway Heaving Caused by High Organic Matter
typeJournal Paper
journal volume23
journal issue2
journal titleJournal of Performance of Constructed Facilities
identifier doi10.1061/(ASCE)0887-3828(2009)23:2(100)
treeJournal of Performance of Constructed Facilities:;2009:;Volume ( 023 ):;issue: 002
contenttypeFulltext


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