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contributor authorTatsuaki Nakato
contributor authorJohn F. Kennedy
contributor authorDonn Bauerly
date accessioned2017-05-08T20:40:41Z
date available2017-05-08T20:40:41Z
date copyrightJanuary 1990
date issued1990
identifier other%28asce%290733-9429%281990%29116%3A1%28119%29.pdf
identifier urihttp://yetl.yabesh.ir/yetl/handle/yetl/23224
description abstractThe circulating water‐pump intake at Iowa Power's Council Bluffs Power Station Unit 3, located along the left concave bank of the Missouri River near Council Bluffs, Iowa, has suffered from chronic fine‐sand shoaling problems both within the intake bays and just outside the intake structure. In order to maintain the pump‐intake bays sediment‐free, an innovative scheme of promoting a deep scour trench in front of the intake is developed using a 1:36‐scale movable‐bed model. On the basis of the model testing results, an array of submerged vanes, comprising two rows of 13, 9‐ft (2.7‐m) wide sheet‐pile vanes, were installed in the prototype in August 1985.The prototype performance of these vanes has been found to be excellent during the past 3.5 yr, and no dredging has been required. The positive riverbed‐scouring approach developed in this study may be a viable solution to resolve persistent sediment‐deposition problems at numerous riverside water intakes.
publisherAmerican Society of Civil Engineers
titlePump‐Station Intake‐Shoaling Control with Submerged Vanes
typeJournal Paper
journal volume116
journal issue1
journal titleJournal of Hydraulic Engineering
identifier doi10.1061/(ASCE)0733-9429(1990)116:1(119)
treeJournal of Hydraulic Engineering:;1990:;Volume ( 116 ):;issue: 001
contenttypeFulltext


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